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金属矿山 ›› 2009, Vol. 39 ›› Issue (01): 81-84.

• 矿物工程 • 上一篇    下一篇

云南普洱某难处理氧化锌矿的选矿试验研究

李玉琼,陈建华,穆枭,魏宗武   

  1. 广西大学
  • 出版日期:2009-01-15 发布日期:2012-02-03

Research on the Beneficiation of a Refractory Zinc Oxide Ore from Puer, Yunnan

Li Yuqiong,Chen Jianhua,Mu Xiao,Wei Zongwu   

  1. Guangxi University, Nanning
  • Online:2009-01-15 Published:2012-02-03

摘要: 针对云南普洱某含泥且含锌方解石的氧化锌矿,对原矿采取了直接浮选法、摇床重选处理后再浮选、磨矿后脱泥再浮选及磨矿前脱泥再浮选等不同的选别方法回收氧化锌。试验结果表明,对含泥量大的氧化锌矿采用直接浮选法,矿石难以选别;采用摇床处理后再浮选法,摇床过程锌损失较大,摇床作业回收率只有50.00%,导致锌总回收率只有40.50%;对原矿磨矿后脱泥处理后再浮选,锌的回收率较重选法提高了18.70个百分点;采用磨矿前脱泥后再浮选的选别流程,较之原矿磨矿后脱泥再浮选,锌品位及回收率分别提高了9.46个百分点和8.30个百分点。采用磨矿前脱泥的氧化锌浮选新工艺已经在工业上获得了成功应用,生产指标稳定,精矿锌品位达到37.21%,锌回收率达到64.97%。

关键词: 氧化锌, 重选, 浮选, 脱泥方法

Abstract: As the zinc oxide ore from Puer, Yunnan, contains both slime and zinc-calcite, different beneficiation methods are used to recover the zinc oxide from the run-of-mine ore, including direct flotation, flotation after tabling, and flotation after de-sliming before or after grinding.The test results show that for the zinc oxide ore containing a large amount of slime, direct flotation is hard to achieve good effect; flotation after tabling can lead to a high zinc loss as the tabling recovery is only 50%, leading to a total zinc recovery of only 40.50%; flotation after de-sliming after grinding can obtain a 18.70% increase in zinc recovery compared with gravity separation; and the process of flotation after de-sliming prior to grinding can achieve a 9.46% and 8.30% increase in zinc grade and recovery respectively compared with the process involving a de-sliming after grinding.Now, the new process of flotation after a de-sliming prior to grinding has achieved successful application in industrial production and achieved stable performances, with the zinc concentrate grading 37.21% at a zinc recovery of 64.97%.

Key words: Zinc oxide ore, Gravity separation, Flotation, Methods of de-sliming