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金属矿山 ›› 2025, Vol. 54 ›› Issue (12): 101-108.

• 矿物工程 • 上一篇    下一篇

石英磨矿行为优化研究

杜孟泽1 聂轶苗1,2 刘淑贤1 王 玲1   

  1. 1.华北理工大学矿业工程学院,河北 唐山 063210; 2.河北省矿业开发与安全技术重点实验室,河北 唐山 063210
  • 出版日期:2025-12-15 发布日期:2025-12-30
  • 通讯作者: 聂轶苗(1979—),女,教授,博士,硕士研究生导师。
  • 作者简介:杜孟泽(2000—),男,硕士研究生。
  • 基金资助:
    河北省自然科学基金项目(编号:E2022209119);河北省中央引导地方科技发展资金项目(编号:236Z3804G);黑龙江省揭榜挂帅项目 (编号:2023ZXJ05A02)。

Study on Optimization of Quartz Grinding Behavior

DU Mengze1 NIE Yimiao1,2 LIU Shuxian1 WANG Ling1#br#   

  1. 1.School of Mining Engineering,North China University of Science and Technology,Tangshan 063210,China; 2.Hebei Province Key Laboratory of Mining Development and Security Technology,Tangshan 063210,China
  • Online:2025-12-15 Published:2025-12-30

摘要: 为提高石英磨矿过程中目标窄级别(0.074~0.038 5 mm)产品的产率并有效抑制过磨,研究以石英纯矿 物为对象,采用卧式球磨机系统考察了介质参数(尺寸、配比、填充率)、物料参数(料球比、磨矿浓度)、磨矿时间及助 磨剂(六偏磷酸钠、氯化铵)的影响。结果表明:在最佳磨矿参数(直径10、15、20 mm陶瓷球质量比3∶5∶3,填充率 20%,料球比0.1,磨矿浓度60%,磨矿时间30 min)下,目标粒级产率较直接磨矿提升25.59个百分点,过磨粒级 (-0.038 5 mm)产率下降23.94个百分点。助磨剂能进一步优化磨矿效果,其中六偏磷酸钠效果优于氯化铵,其用量 为0.5%的情况下,目标粒级产率可在参数优化基础上再提升6.88个百分点,过磨粒级产率再降低3.97个百分点。 最终,通过全流程优化获得了目标粒级产率达83.96%、过磨粒级产率仅5.05%的理想产品,显著提升了资源利用率。 研究为石英的高效选择性磨矿提供了可靠的技术途径。

关键词: 石英 介质尺寸 介质级配 介质填充率 料球比 助磨剂六偏磷酸钠

Abstract: To increase the yield of the target narrow-size fraction (0.074~0.038 5 mm) and effectively suppress over grinding in the quartz grinding process,this study systematically investigated the effects of medium parameters (size,ratio,fill ing rate),material parameters (material-to-ball ratio,grinding concentration),grinding time,and grinding aids (sodium hex ametaphosphate,ammonium chloride) using a horizontal ball mill and pure quartz.The results showed that under the optimal grinding parameters (the mass ratio of ceramic balls with diameters of 10,15 and 20 mm of 3∶5∶3,filling rate of 20%,materi al-to-ball ratio of 0.1,grinding concentration of 60%,grinding time of 30 min),the yield of the target fraction increased by 25.59 percentage points,while the over-ground fraction (-0.038 5 mm) decreased by 23.94 percentage points compared with direct grinding.Grinding aids further enhanced the performance,in which sodium hexametaphosphate outperformed ammonium chloride,and at its optimal dosage (0.5%),the target fraction yield increased by an additional 6.88 percentage points,and the over-ground fraction yield decreased by a further 3.97 percentage points.Through the entire process optimization,a final prod uct with a target fraction yield of 83.96% and an over-ground fraction yield of only 5.05% was achieved,significantly impro ving resource utilization rate.This study provides a reliable technical pathway for the efficient and selective grinding of quartz.

Key words: quartz,medium size,medium gradation,medium filling rate,material-to-ball ratio,grinding aid sodium hex ametaphosphate

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