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金属矿山 ›› 2026, Vol. 55 ›› Issue (2): 128-137.

• 矿物工程 • 上一篇    下一篇

BPMA 导向的某高硫铝土矿浮选脱硫工艺研究

李红妍1 唐 云1 王在谦2 邓政斌1 方添添1 秦 浪3 钱万拾1 石韬炜1   

  1. 1. 贵州大学矿业学院,贵州 贵阳 550025;2. 贵州成黔矿业科技有限公司,贵州 贵阳 550000;
    3. 贵州铝业集团有限公司,贵州 贵阳 550001
  • 出版日期:2026-02-15 发布日期:2026-03-03
  • 通讯作者: 邓政斌(1986—),男,讲师,博士。
  • 作者简介:李红妍(2002—),女,硕士研究生。
  • 基金资助:
    贵州省科技计划项目(编号:黔科合基础-[2024]青年140)。

Study on Flotation Desulfurization Process of a High-Sulfur Bauxite Guided by BPMA

LI Hongyan1 TANG Yun1 WANG Zaiqian2 DENG Zhengbin1 FANG Tiantian1 QIN Lang3    QIAN Wanshi1 SHI Taowei1#br#   

  1. 1. School of Mining,Guizhou University,Guiyang 550025,China;2. Guizhou Chengqian Mining Technology Co. ,Ltd. ,
    Guiyang 550000,China;3. Guizhou Aluminum Industry Group Co. ,Ltd. ,Guiyang 550001,China
  • Online:2026-02-15 Published:2026-03-03

摘要: 为实现贵州某高硫铝土矿的高效利用,本研究采用基于扫描电子显微镜(SEM)与能谱仪(EDS)的工艺
矿物学自动分析系统(BPMA),对Al2O3 品位为56. 16%、硫含量达4. 58%的矿石进行了系统的工艺矿物学研究。研
究精确揭示了铝、硫元素的赋存状态与主要矿物的嵌布特征,并以此为指导进行浮选脱硫试验。通过条件优化,确定
了最佳工艺参数:磨矿细度-75 μm 占85%、矿浆pH=6、以CuSO4 为活化剂(50 g/ t)、组合捕收剂丁基黄药+丁铵黑药
(30+120 g/ t)。最终,采用1 粗2 精3 扫闭路浮选流程处理,成功获得了产率为82. 85%、Al2O3 品位为65. 05%、硫含
量降至0. 48%、铝硅比(A/ S)为12. 19 的优质铝精矿,其中Al2O3 回收率达95. 96%、脱硫率为91. 29%。研究表明,
BPMA 技术能为浮选工艺开发提供关键的矿物学依据,本研究为此类高硫铝土矿的高效分选与资源化利用提供了可
靠的技术方案和实践借鉴。

关键词: 一水硬铝石 黄铁矿 脱硫浮选 BPMA 工艺矿物学

Abstract: To achieve the efficient utilization of high-sulfur bauxite from Guizhou,this study employed process mineralogy
analysis system (BPMA) based on Scanning Electron Microscopy (SEM) and Energy Dispersive Spectroscopy (EDS) to conduct
a systematic mineralogical characterization of an ore sample assaying Al2O3 of 56. 16% and S of 4. 58%. The study accurately
revealed the occurrence states of aluminum and sulfur,as well as the dissemination characteristics of the main minerals,
which guided the subsequent flotation desulfurization tests. Through condition optimization,the optimal parameters were determined
as follows:grinding fineness of 85% passing 75 μm,natural pulp (pH=6),CuSO4 as activator (50 g/ t),and butyl xanthate
mixed with ammonium butyl aerofloat as combined collector (30+120 g/ t). A closed-circuit flotation flowsheet consisting
of "one roughing,two cleaning,and three scavenging" stages was finally adopted,successfully producing a high-quality aluminum
concentrate with a yield of 82. 85%,containing 65. 05% Al2O3 and only 0. 48% S,corresponding to an aluminum-silicon
ratio (A/ S) of 12. 19. The Al2O3 recovery and desulfurization rate reached 95. 96% and 91. 29%,respectively. This research
demonstrates that BPMA technology can provide critical mineralogical basis for flotation process development,offering a reliable
technical solution and practical reference for the efficient beneficiation and utilization of such high-sulfur bauxite resources.

Key words: diaspore,pyrite,desulfurization flotation,BPMA,process mineralogy

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