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Metal Mine ›› 2008, Vol. 38 ›› Issue (10): 48-51.

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Research & Design of the Beneficiation Process for Separate Quality Improvement & Impurities Reduction of Iron Concentrate and Its Application Practice

Luo Liqun1,2,Fang Yong3,Chen Dianzhu4,Ren Jinrong5,Yang Xinyue5   

  1. 1.Wuhan University of Technology;2.Mineral Resources Processing and Environment Laboratory of Hubei;3.Changsha Research Institute of Mining and Metallurgy;4.Changsha Engineering & Research Institute of Nonferrous Metallurgy;5.Industry and Mining Product Trading Company of Shanxi
  • Received:2008-08-10 Online:2008-10-15 Published:2011-07-13

Abstract: There are a number of small sized magnetite ore concentrators in a region in Shanxi, which produce iron concentrates by low intensity magnetic separation that have an iron grade of only 61%~58% but an SiO2 content as high as 12%~15%, not conforming to the guideline of good burden preparation for blast furnace iron-making and seriously affecting their sales. Based on the experimental research and in light of the local real conditions, a separate concentrator for their upgrading has been designed and built for a centralized treatment of these iron concentrates, which adopts a process consisting of reverse flotation, middling regrinding and low magnetic separation, and a high efficient anionic collector LP-4 that can be used in normal temperature. Now, this separate concentrator is running stably and has a good adaptability. It is capable to raise the iron grade of the concentrate to 67.2%~66.5%and reduce the SiO2 content to 5.2%~5.8%, demonstrating a good effect of quality improvement and impurity reduction.

Key words: Iron concentrates of low intensity magnetic separation, Quality improvement and impurities reduction, Separate upgrading concentrator, Reverse flotastion, High efficient collector LP-4