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金属矿山 ›› 2025, Vol. 54 ›› Issue (9): 57-62.

• 采矿工程 • 上一篇    下一篇

深部泵房硐室裂隙浆液扩散机制及“锚注”修复技术 

聂济刚1   辛亚军2,3   白克新1   王  飞1   常晓亮2    

  1. 1. 永煤集团股份有限公司顺和煤矿,河南 永城 476600;2. 河南理工大学能源科学与工程学院,河南 焦作 454000; 3. 煤炭安全生产与清洁高效利用省部共建协同创新中心,河南 焦作 454000
  • 出版日期:2025-09-15 发布日期:2025-09-30
  • 作者简介:聂济刚(1982—),矿长,高级工程师。
  • 基金资助:
    国家自然科学基金项目(编号:51374091);河南省重点研发与推广专项(科技攻关)项目(编号:232102321132)。 

Mechanism of Slurry Diffusion in Crack and "Anchoring Grouting" Repair Technique on Deep Pumping-room Chamber 

NIE Jigang 1   XIN Yajun 2,3   BAI Kexin 1   WANG Fei 1   CHANG Xiaoliang 2    

  1. 1. Shunhe Coal Mine,Yongcheng Coal Group Co. ,Ltd. ,Yongcheng 476600,China; 2. School of Energy Science and Engineering,Henan Polytechnic University,Jiaozuo 454000,China; 3. Collaborative Innovation Center of Coal Work Safety and Clean High Efficiency Utilization,Jiaozuo 454000,China
  • Online:2025-09-15 Published:2025-09-30

摘要: 由于深部大断面硐室断面尺寸大、应力水平高,使得硐室围岩控制难度加大,通过对顺和煤矿-702 m 水 平主排水泵房围岩变形破坏特征实测及失稳原因分析,研究了深部大断面硐室围岩裂隙不同注浆液扩展规律与影响 机制,提出了深部大断面硐室“高强注浆锚索+壁后注浆”加固方案,并进行了现场工业试验。 结果表明:深部大断面 硐室围岩松动圈呈非规则形态,围岩松动范围较大,近巷道围岩破碎程度高,两帮松动范围最大、顶板次之、底板较小, 不同位置岩体破碎特征差异较大;大断面硐室围岩失稳原因为应力水平高、围岩强度低、裂隙水浸入、支架结构差与 底板无支护,裂隙扩展发育至贯穿是围岩失稳的主控因子;注浆压力对围岩裂隙中浆液扩散影响大于水灰比,水灰比 与注浆压力越大,浆液扩散半径越大,且浆液切向扩展范围大于径向,最佳水灰比与注浆压力分别为 0. 7 与 1. 5 MPa; 高强注浆锚索实现了轴向与环向锚固均匀受力承载,采用设计的“高强注浆锚索+壁后注浆”加固方案后,顶板最大下 沉量为 8 mm,两帮最大收敛量达 24 mm,围岩控制效果显著。 

关键词: 深井巷道  大断面硐室  松动圈  浆液扩散  “锚注”加固  稳定性 

Abstract: Due to the large section size and high stress level in the deep chamber,it is more difficult to control the surrounding rock of the chamber. This paper studied the expansion law and influence mechanism of different grouting fluid in the surrounding rock cracks of the deep large-section chamber by measuring deformation failure characteristics and analyzing instability causes of surrounding rock of main drainage pumping-room chamber in Shunhe Coal Mine -702 m horizontal. The reinforcement scheme of " high strength grouting cable+wall grouting" for deep large-section chamber was put forward,and the field industrial test was carried out. The results showed that surrounding rock loose circle in deep large-section chamber was irregular,the loose range was large,the surrounding rock broken degree was high near the gateway:two-side loose range was the largest,the roof second,the floor was small,and rock breaking difference were large in different locations. The causes of surrounding rock instability in large-section chamber were high stress level,low surrounding rock strength,fissure water immersion,poor support structure and no support in floor,and fracture propagation penetration was the main control factor of surrounding rock instability. The influence of grouting pressure on slurry diffusion in surrounding rock cracks was greater than that of water-cement ratio. The larger the water-cement ratio and grouting pressure was,the larger the slurry diffusion radius was,and the tangential expansion range of slurry was larger than that of radial. The optimal water-cement ratio and grouting pressure were 0. 7 and 1. 5 MPa respectively. The high-strength grouting cable achieved uniform anchoring bearing in axial and circumferential. After the reinforcement scheme of " high-strength grouting cable + wall grouting" was carried out,the maximum roof subsidence was 8 mm and the maximum two-side convergence was 24 mm,and the surrounding rock control effect was remarkable. 

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