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金属矿山 ›› 2025, Vol. 54 ›› Issue (10): 90-96.

• 矿物工程 • 上一篇    下一篇

辽宁某铁矿石磁浮联选新工艺试验研究

毕佳宝1,2,3 刘 杰1,2,3 唐志东1,2,3 李艳军1,2,3   

  1. 1. 东北大学资源与土木工程学院,辽宁 沈阳 110819;2. 矿物加工科学与技术全国重点实验室,辽宁 沈阳 110819;
    3. 难采选铁矿资源高效开发利用技术国家地方联合工程研究中心,辽宁 沈阳 110819
  • 出版日期:2025-10-15 发布日期:2025-11-06
  • 通讯作者: 李艳军(1972—),男,教授,博士,博士研究生导师。
  • 作者简介:毕佳宝(2000—),男,硕士研究生。
  • 基金资助:
    “十四五”国家重点研发计划项目(编号:2021YFC2902401)。

Experimental Study on a Novel Magnetic-Flotation Combined Process for An Iron Ore in Liaoning

BI Jiabao1,2,3 LIU Jie1,2,3 TANG Zhidong1,2,3 LI Yanjun1,2,3   

  1. 1. School of Resources and Civil Engineering,Northeastern University,Shenyang 110819,China;2. State Key Laboratory of Mineral
    Processing Science and Technology,Shenyang 110819,China;3. National-Local Joint Engineering Research Center for
    High-Efficiency Development and Utilization of Refractory Iron Ore Resources,Shenyang 110819,China
  • Online:2025-10-15 Published:2025-11-06

摘要: 针对辽宁某选矿厂难选铁矿石分选效率低、金属流失严重的问题,提出了“一段磨矿—1 弱1 中1 强磁
选—二段磨矿—反浮选”新工艺。通过采用1 中1 强磁选有效降低了尾矿品位,并在浮选前增加二段磨矿以精确控制
入浮粒度,显著提升了系统分选效率。试验结果表明:对于TFe 品位29. 33%的原矿,经磁选预富集可获得TFe 品位
37. 51%的磁选精矿,尾矿品位降至4. 88%,磁选段回收率达95. 83%;对该磁选精矿进行浮选条件优化与开路、闭路试
验,最终获得TFe 品位65. 12%、全流程总回收率72. 57%的最终精矿。与原工艺相比,新流程磁选尾矿品位降低8. 04
个百分点,总回收率提高11. 66 个百分点,有效减少了铁资源流失,对提高选厂经济效益和资源利用率具有实际意义。

Abstract: Aiming at the problems of low separation efficiency and severe metal loss in treating refractory iron ore at a beneficiation
plant in Liaoning,a new process of "one-stage grinding,one-stage low-intensity magnetic separation,one-stage medium-
intensity magnetic separation,and one-stage high-intensity magnetic separation,two-stage grinding and reverse flotation"
was proposed. The application of one-stage medium-intensity and one-stage high-intensity magnetic separation effectively reduced
the grade of tailings,and the addition of two-stage grinding before flotation precisely controlled the feed particle size for
flotation,significantly improving the system separation efficiency. Test results showed that for run-of-mine ore with a total iron
grade of 29. 33%,a magnetic separation concentrate with a total iron grade of 37. 51% was obtained through magnetic preconcentration,
the grade of tailings was reduced to 4. 88%,and the recovery rate in the magnetic separation stage reached
95. 83%. Through the optimization of flotation conditions and open-circuit and closed-circuit tests on this magnetic separation
concentrate,a final concentrate with a total iron grade of 65. 12% and an overall process total recovery of 72. 57% was ultimately
obtained. Compared with the original process,the new flow sheet reduced the grade of tailings from magnetic separation
by 8. 04 percentage points and increased the overall recovery by 11. 66 percentage points,effectively reducing iron resource
loss,which has practical significance for improving the economic efficiency and resource utilization rate of the beneficiation
plant.

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