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金属矿山 ›› 2009, Vol. 39 ›› Issue (01): 127-130.

• 机电与自动化 • 上一篇    下一篇

CJ411型颚式破碎机机架开裂修复研究

徐红玉,肖琪聃,杨靖宇,沈贵平   

  1. 河南科技大学
  • 出版日期:2009-01-15 发布日期:2012-02-03

Research on Repairing the Cracked Frame of CJ411 Jaw Crusher

Xu Hongyu,Xiao Qidan,Yang Jingyu,Shen Guiping   

  1. Henan University of Science & Technology
  • Online:2009-01-15 Published:2012-02-03

摘要: 采用有限元分析软件ANSYS对CJ411型颚式破碎机机架进行数值模拟,分析机架开裂破坏的主要原因。意外载荷促使破碎机处在高应力条件下的铸造构件缺陷演化萌生裂纹,长期超负荷运转的高交变应力环境方便了裂纹快速增长,最终导致机架疲劳失效。在此基础上提出了机架结构修复改进措施: 将高应力区域的铸造构件用碳钢焊接件代替;横梁和机架的连接由焊接改为螺栓连接。修复前后机架数值模拟对比分析表明,机架应力分布合理,既充分利用材料特性,又大大降低断裂失效概率,改进效果明显。本研究不仅解决了实际问题,更为颚式破碎机生产设计单位在机架设计优化方面提供参考。

关键词: 颚式破碎机, 机架, 优化分析, 有限元分析

Abstract: The finite element analysis software ANSYS was used in the numerical simulation of the frame of CJ411 jaw crusher and the main causes leading to the frame crack were analyzed.The accidental load led to the evolution of the defects in the casting member of the crusher that was under a high stress, leading to the flaws.The high alternating stress produced in long term overload operation facilitated the rapid growth of these flaws, finally leading to the fatigue failure of the frame.On this basis, measures for repairing and improving the frame structure were proposed: to use welded carbon steel components to replace the casting members in the high stress zone and to change the welding to bolting for the connection between the beam and side plates.The numerical simulation comparative analysis of the frame before and after the repair indicates that the repaired frame has a rational stress distribution, and the measures have not only fully utilized the material properties but also greatly reduced the fracture failure probability, achieving a remarkable improvement.This research has not only solved the practical problem but also provides a reference to the frame design optimization of jaw crusher.

Key words: Jaw crusher, Frame, Optimization analysis, Finite element analysis